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INNOVATION                                                                                                                                                                                          JSW ENERGY BOLT  |  ISSUE 1W ENERGY BOLT  |  ISSUE 1
                                                                                                                                                                                                            JS
        What were the challenges encountered?                   overwhelmed by the results in the form of                      How was the problem solved?                             How the team felt on the problem being

                                                                savings and learning.                                                                                                  resolved?
        First challenge to proceed with the above                                                                              In-House Generator Stator Chemical

        modification was minimum support                        Any specific aspects which you may like                        Cleaning by introducing Nitrogen (N2)                   The entire team had felt extremely happy
        available from OEMs. All the activities                 to mention?                                                    bubbling arrangement in SCW tank to                     as the problem was solved in-house

        planned and executed by in-house team                                                                                  reduce Dissolved Oxygen in stator water.                without disturbed the stator coil system.
                                                                 ESP and Ash handling plants are common
        comprising of personnel from different                                                                                 This Chemical cleaning was process was                  Management had given positive response
                                                                in most of the JSW establishments, as the
        departments.                                                                                                           including selection of cleaning chemical,               & supported in all aspects to achieve the
                                                                loop holes were identified, solutions were
                                                                                                                               circulation pump, corrosion inhibitors,                 results.
        Impact of solution to the business?                     ideated with the help of domain expertise.
                                                                                                                               online monitoring of chemical & process
                                                                Implemented various methodologies to                                                                                   Any specific aspects which you may like
        a.  Savings in Hopper heater Power                                                                                     parameters, balancing of N2 pressure &
                                                                overcome the problems and hence can                                                                                    to mention?
        consumption is 61 KWH resulted in                                                                                      DO in stator water system. In this process
                                                                be institutionalized.
        INR18.27 Lacs/Annum.                                                                                                   injection of chemical solution was                      Management supported well and they

                                                                                                                               continuously done for nearly 72 hrs. at                 believed in our team to carry out such a
        b.  Savings in AHP Power consumption is
                                                                          Team Members                                         inlet of stator coil, in parallel with removal          critical activity without. After seeing the
        28 KWH resulted in INR 8.38 Lacs/ Annum.

                                                                   Abhishek Nayak                                              of contaminants (copper oxides) at outlet               results, the same activity was repeated in
        c.  Savings in ESP field power                                                                                         by using Mixed Bed (MB) in SCW system.                  Jaigarh plant also.
                                                                   Rajendran S
        consumption is 250 KWH/Unit resulted in                                                                                High pure Nitrogen (N2) was used for
                                                                   Meenakshi Sharma
        INR  70.73 Lacs / Annum/Unit.                                                                                          blanketing to reduce the DO in stator                             Team Members
                                                                   Madhukar D

        Total Savings INR 389.32 Lacs / Annum for                  Bheemesh D                                                  water system.  The overall activity was                    Shashi Bhushana  B
                                                                                                                               carried out in coordination with
        4X300 MW Units was achieved.                                                                                                                                                      Srinivas  Amjuri
                                                                                                                               Chemistry, Operation and Maintenance                       Chetan  Kumar SV
        Savings achieved with zero investment in                Innovative Idea :                                              dept.  Total Cost incurred for the said

        AHP and ESP fields and with a small                     Generator Stator                                               activity was Rs. 5000/-.
        expenditure of INR 3 lakhs for hopper                   Chemical

        heaters sensors                                         Cleaning-300 Mw                                                Impact of solution to the
                                                                                                                               business?
        How the team felt on the problem being                  How and Why was the problem

        resolved?                                                                                                               This had saved cost of generator
                                                                identified?
                                                                                                                               stator coils and cost of cleaning
        Since the project taken up was a process                Increasing trend in 300 MW Generator                           by OEM is around Rupees 120
        improvement and energy saving task,                     stator coil differential pressure indicating                   Lacs/Unit. And Generator

        team comprising of                                      the flow restrictions within the stator                        performance was improvement a
        Mr. Abhishek Nayak,                                     cooling water channels. Observed there                         lot. Generator stator DP reduced

        Mr. Rajendran,                                          was continuous increasing trend in Stator                      from 0.23 to 0.15 Mpa, stator
        Ms. Meenakshi Sharma,                                   coil dP from 0.15 to 0.23 Mpa and                              water flow improved from 46 to 55

        Mr. Madhukar and                                        reduction in stator water flow from                            TPH.
        Mr. Govindaraju a totally cross functional              55 to 46 TPH.

        team from different disciplines was


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